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greendane

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greendane last won the day on June 10

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About greendane

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    Stanwood, WA (Puget Sound)

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  1. Would love to see pics Randy when you have time. Thanks!
  2. @Randy JonesIf by regular you mean the center position, you're right. It wasn't in the third (aft) position. I went for another sail last night and was able to tack ok. The waves were a lot less so my momentum carried me around a little easier. Still pretty slow to come about though. I'm sure with both sails it would do what it's supposed to. I'm also pretty sure that if I was a more experienced sailor I'd have less issues. I don't have a halyard on my laced sails so I typically just furl them to "take them down". In the conditions I've been in single-handed, I am pretty uneasy moving forward to fiddle with just about anything (I didn't even like flipping out the fender on that side.) I also have an odd mast repair where I essentially wrapped a 1/2" thick box around a spot in the wood (hollow square) mast that was de-laminating. That box, though tapered, presents a hang-up point for raising and lowering. I've thought about trying this to see if it would help. But I wonder if under pressure I could get it to come down easily or not.
  3. And for reference, this is a pretty good drone video showing the area I was at (and usually go to).
  4. @PeterP Yup. Next time I see the whitecaps coming, I'm firing up the motor, furling the sail and coming the rest of the way back by motor and calling it a day sooner rather than later. And doing better forecasting on the wind. (The forecast was there, I just didn't make the xtra effort to confirm it.) There's a good bit of respect to be had for the Puget Sound. While there is a lot of protection, there is also a lot of potential for crazy weather. This is an extreme example:
  5. I gave myself a good scare this weekend. And learned a few adrenaline enforced lessons. Account of novice below... I opened my windy app and it was a buggy so I figured I'd just read live conditions when I got to the ramp. (Lesson 1: sort out the forecast first.) There was a stiff breeze but generally speaking, if there aren't white caps and the waves aren't really rocking, I'm pretty safe (only sailing with the one sail in the middle position mind you). Started off fine and fun. Got some spray as I was close hauled heading out. Moving faster than I've ever gone and kept my hand on the sheet the whole time to be ready for any gusts. I got out a little over a 1/2 mile and things picked up. I tried tacking but the head wind wouldn't let me get around until the 3rd try. (I'd just stall in irons). I wasn't comfortable moving to a reach > and turning through run/gibe in those conditions. (Would appreciate any wisdom here. It wasn't a lack of speed. The wind just stopped me dead in my tracks.) So after the third (and successful) tack attempt, I turned to a broad reach and I was on a plane off and on. Definitely the fastest I've ever gone in my CY17. I'm guessing I was close to 8 knots on a plane and when surfing down the side of the waves. Part of it was good fun. But the wind was growing and the dock/ramp faces winward. The part that wasn't fun was when I had to turn on a run to get back to the dock as the wind picked up. (Maybe 20-25 knots if the post-mortem assessment on the Windy app is true). The angle of the waves (no more than 2 ft I think) and the wind made it feel really unstable, even though I had the sail forward of the mast a bit. I was 300 yards out at this point. The ramp was really busy as everyone was getting off the water. I ended up using my motor (2hp Honda) to have more consistent speed. I unhooked the sheet and the sprit, let the sail flog (it was too precarious to wrap it). I pointed into the dock, found a hole between all the big boats, shut the motor at the right time and glided to the dock. I clung to the cleats, threw my fenders out (didn't have time for that earlier), tied off and called it a day. Counting my blessings with every step to my truck and trailer. I was rattled enough to forget to pull up the rudder and scuffed the bottom of it when I pulled the boat out. Bummed about that. Several lessons there, and I am a willing student for any advice from you seasoned folks.
  6. Hi all--for the next few months until I have my new masts, I only have one. I sailed it (my CS17) last year in the center position and it worked fine. I've generally run with the mizzen sail only, though I have laced on the main a couple of times. The main sail encroaches on visibility and the sprit-boom swings just at eye level. I am curious though (and new to sailing--this is the only boat I've ever sailed), if I put the single mast and sail in the bow, how would the boat behave? More or less likely to heel or capsize? Always wanting to turn so I'd be fighting with the tiller? I really don't understand the dynamics and prefer to get some theory and feedback before doing any trial and error. Thanks.
  7. Trailer for Core Sound 17

    I found a Galvanized Calkins 1000 lb capacity trailer for super cheap ($250). I took off the pivoting roller racks (there were 2 u-shaped beefy things) and replaced with some brand new 8" wide rollers that I found on Craigslist for $15 each (instead of $40) and scabbed one 4" off my old trailer. My bunk brackets will arrive tomorrow and I'll be wrapping either 2X4 or 2X6 with carpet for the bunks. Replaced the cable in the winch with a strap, new safety chain, lights, and replaced and repacked the wheel bearings. I added a cross-member L-beam to the back to provide a home for the first roller. Am cleaning up a few minor rust spots and with any luck, I'll be able to get the boat flipped and on the trailer this weekend.
  8. Core Sound 17 keel maintenance

    Funny you shoujld say this. I have one rather perfectionistic child and as we're wrapping up the school year I've had to instill an old mantra that was passed on to me: "Done is good." It's so true.
  9. Core Sound 17 keel maintenance

    In closing, I just would like to thank all of you for your input along the way. I honestly couldn't have done it without you. @PAR -- you were especially willing to share your expertise and take the time to hammer out all those pixels to help me out. @PaulSmith--thanks for your local perspective. We'll need to connect sometime. @Hirilonde--thanks for weighing in as well. You catch the little things. They were useful. More to come I am sure, but much thanks for your help to get me to this point. All the best!
  10. Core Sound 17 keel maintenance

    The main keel rub strip was the easiest. It was a little warped so I had to gently work it a bit straighter, but it flexed enough that it trued up easily with the screws. Was only off about 1/2" over the 10' length. The setback here was providing the wrong measurements to the metal shop. Ripping the 1/4" off the length of it with my table saw as time consuming. I had to build a jig of sorts to keep the bar flat and into the table, but also square to the blade. Also had to keep the waste section down and still, which I did by clamping a couple of thin paint sticks to the fence to hold just enough down pressure. Shaping the taper and curve at the end proved more work than I liked. I don't have a band saw, so I tried a grinder. It mostly clogged up and didn't actually work that fast. I ended up cutting the bulk off with a hacksaw, and using a zip cutter to essentially router off the remaining. That went faster than the hand filing, which is what I used to finish it off. I was going to try to form the front down over the nose of the keel. I did it, but it never took the form well so I had to straighten it back out. It never went back the way it started. So as you can see from the pics above, it's munged up a tad.
  11. Core Sound 17 keel maintenance

    While I was at it, I cleaned up and put an extra coat of epoxy on the centerboard. It seemed a little thin in places. Also cleaned out the epoxy and paint drips out of the trunk. Next time I would be more careful to mask no just the centerboard, but the trunk as well. Had to reach in with a hacksaw blade to cut away a couple drips that were hard enough to leave scratches on the centerboard when it pivoted.
  12. Core Sound 17 keel maintenance

    Transitions: So one of the many things I didn't do well was re-engineer the keel to transition to the stem. And the same thing on the skeg to the keel transition. I should have tapered these down to nothing instead of stopping short. At the time, I guess I thought those little skinny bits would be too flimsy to manage. It was only slightly odd without the rub strips, but with them, the transitions became more obvious. Compared to what I started with, it's better off than it was. But I'd do it differently next time. Some of the caulking here is a little sloppier than I like, but I didn't want to take more away from the seal. And so it is what it is.
  13. Core Sound 17 keel maintenance

    Well, it's done. Will post pics in a while. The jig for ripping the tube worked perfectly. It did take some work with a file to round over cut edges. And the bend was pretty easy too. Just a little at a time seemed to work. I was surprised but it never expanded the radius with the gentle curve. The downside is that I could never get the radius to collapse to align to the tighter radius on the front. So there was a little more lip there then I liked but I just made sure the 3m adhesive filled it in. All in all, I think it will serve its purpose and I am more than glad to be done. I'll post some lessons learned later too.
  14. Core Sound 17 keel maintenance

    So nothing ever seems to go as smooth as we hope. Or as I hope anyway. With 5052 aluminum they have to manufacture "flat bar" from a sheet. For the wide one it was fine though did have a slight bow. I straightened it out gently pulling it over a saw horse with firm but mild pressure. The 3/4" piece is another story. It came out with a bow, a twist and a warp. The bow was managed easily enough. And the twist took some twisting in the other direction while clamped. The warp was another story. I started by running it under a mallet. No real movement. But then I clamped it to a table and started working it a. It at a time. It'll be fine. Total of about 45 minutes farting around. Chapter two has to do with me giving them dimensions for the larger one that were a 1/4" too wide. Ugh. So I'm going to build a jig on my table saw to cut that last bit off. Hope that goes as easy as the rest.
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